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1985
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1985 was quite a year. For one thing it almost
bankrupted me. You see during the course of those 12 months I travelled
almost 12,000 miles behind steam locomotives on the main line.
At times it was quite hard work.
1985 was the year of the 150th Anniversary of the Great Western Railway.
Sadly, the GW150 celebrations never quite lived up to the hype. Then
there were 22 Scarborough Spa Expresses to do. Steam out of Marylebone
was just beginning. There were a few trains in Scotland to do. Add to
these the normal round of Cumbrian Mountain Expresses etc. and you can
see how the mileage (and expense) added up.
Still, despite everything, I'm glad I did it. I couldn't even contemplate
it at today's prices!
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The first stirrings of GW150
Anyone who experienced it (I'm tempted to say
the full horror of it!) will never forget that 1985 was the year of
the 150th Anniversary of the Great Western Railway.
The events celebrating GW150 were spread throughout much of the year
involving a great deal of what, on the face of it, sounded like some
very attractive main line steam activity. The reality proved to be somewhat
different!
Actually, to use the word 'horror' isn't quite fair. Much of what we
experienced was quite good and there were one or two outstanding runs
to offset the disasters.
Sadly, the running behind 4930 'Hagley Hall' on 2nd February 1985 although
not a disaster could not in any way be described as even 'quite good',
it was dire in the extreme!
The train was the first over yet another new route for steam. Starting
from Newport we ran through Chepstow to Gloucester then headed for Swindon
over Sapperton.
With a train of just 8 coaches we expected the Hall to do well on Sapperton
bank which steepens to 1 in 60 but, thanks to the crew working the engine
very easily (I don't believe that the regulator was out of the pilot
valve at any time) we fell to just 10 mph on this section.
This is how the Hall sounded climbing the last of the 1 in 60 gradient
and entering Sapperton Long Tunnel where the gradient eases.
And the excuse for this 'performance'? There were to be a series of
steam hauled shuttle trains between Gloucester and Swindon during the
summer months and the powers that be wanted to see how easily the Hall
could cope with the load! Nice of us to pay for them to practice wasn't
it.
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4930
climbing Sapperton Bank. 2nd February 1985 |
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SLOA stewards (nearly) always remained
calm!
On 23rd February 1985 Black 5 44767 and Jubilee
5690 'Leander' double headed the Thames - Eden Express which was steam
hauled from Manchester to Carlisle.
With two engines to service frequent water stops were the order of the
day. Despite having taken water at Blackburn we had another water stop
at Long Preston. In this recording the pair are heard departing and
heading for Settle Jc.
So, what does this have to do with SLOA Stewards?
Those of you who were regular travellers on specials at this time will
recall that there were always plenty of stewards on hand on these special
trains, indeed sometimes it seemed that there were more stewards than
passengers and at water and photo stops stewards were positioned at
various points to ensure that none of the passengers trespassed on running
lines.
Well, as you will hear, it seems that the tenders were topped up far
sooner than at least one steward, who had best remain nameless, expected!
Fear not, he wasn't lost forever, he was waiting for us at Garsdale
when we stopped there for water having cadged a lift with a lineside
photographer
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44767
& 5690 departing Long Preston. 23rd February 1985 |
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A Jubilee in Scotland
Jubilee 5690 'Leander' and Black 5 44767 after
having worked northbound over the Settle-Carlisle route had continued
into Scotland.
The pair were booked to work the Fair Maid from Edinburgh to Perth and
back on 30th March 1985 with 'Leander' working the outward journey and
the Black 5 taking the return.
In this recording the Jubilee is heard recovering from a PWS near Larbert
and starting on the short climb to Plean.
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5690
near Larbert. 30th March 1985 |
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GW150 - Steam to Plymouth
Easter Sunday 7th April 1985 was confidently
expected to go down in the history of railway preservation as a very
memorable date and, indeed, it did, though not for the right reasons.
One of the main events was the planned 6 steam hauled trains on the
main line between Bristol and Plymouth including the steep South Devon
banks and the first of these trains ran on that date.
Motive power for this first train was King 4-6-0 6000 'King George V'
and 4-6-0 7819 'Hinton Manor' and, in true Great Western tradition,
the train engine was coupled in front of the assisting loco.
This recording was made as, just a few minutes late, the pair at the
head of 13 fully laden coaches depart from Bristol Temple Meads as a
band on the platform plays what later proves to be some very appropriate
music. Leaving Bristol almost every vantage point was packed with spectators.
We must have presented a magnificent sight and one group of onlookers
burst into spontaneous applause as we passed
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6000
& 7819 departing from Bristol. 7th April 1985 |
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Later, after a satisfactory run from Bristol
with speeds in the mid 60's it became apparent as we approached Taunton
that all was not well with the King. Smoke could be seen emerging from
underneath the right hand side of the tender and, once we had stopped
in the station for our booked water stop the King was detached and moved
to the bay platform. On the tender, the right hand leading axlebox had
run hot and the damage was serious enough to preclude the King continuing
further west. While we passengers were very disappointed the King's
support crew members were devastated and a few had tears in their eyes.
Meanwhile we were left with 7819 at the head of an almost 500 ton train
and lots of climbing ahead.
The decision was taken to allow the Manor to continue but with diesel
assistance on the banks. Two Class 37s appeared and were coupled at
the rear of the train, initially as far as Tiverton Jc. to provide assistance
over Whiteball. The plan was that the Manor would then run unassisted
from Tiverton Jc. to Newton Abbot where the diesels would be reattached
for the South Devon banks.
Over Whiteball, despite the diesel assistance the crew on the Manor
were doing their best to provide some entertainment and, after the diesels
had been detached at Tiverton Jc. we had some sprightly running down
to Exeter.
They say that lightning never strikes twice in the same place but, on
that Sunday, it did. Approaching Exeter we were stopped by signals at
Cowley Bridge Jc. Having got the road 7819 soon has the train under
way but we were all too aware what the clearly audible high pitched
whistle indicated.
You guessed it, another overheated axelbox. What was even more remarkable
was that the offending axelbox was the right hand leading one on the
Manor's tender the same one that had affected the King.
And that was the end of steam haulage. We continued with diesel haulage
to Plymouth in a very sombre mood, especially since some of us had booked
to do the return journey from Plymouth to Bristol on the following day.
So, why was the music at Bristol so appropriate? Well, 'Wish me luck
as you wave me good-bye' was reputed to be the tune that was played
at Southampton as the 'Titanic' departed on her maiden voyage.
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Came the dawn.
On arrival at Plymouth North Road station on the morning of Easter Monday
8th April 1985 we were delighted to discover that, not only had 'Hinton
Manor' been repaired but that 4930 'Hagley Hall' had arrived having
travelled overnight from the Severn Valley Railway.
What was not quite so good was the quality of the coal provided for
the journey. Someone had ordered the wrong grade of coal and the small
stuff delivered caused problems for the fireman. Still, we were getting
our steam hauled run where, 12 hours before it had seemed most unlikely.
So, 15 minutes later than planned, in somewhat higher sprits than we
had expected to be, we departed from Plymouth for Bristol.
The first of the South Devon banks, Hemerdon, is encountered just a
few miles from the start. Falling gradients soon after leaving Plymouth
usually allow the bank to be approached at a reasonable speed but we
were denied this by signal checks out to Laira and passed Plympton at
the foot of the bank with speed in the low 30's.
Once on to the bank itself and on a gradient of 1 in 41 speed fell with
alarming rapidity. What we didn't know was that Manor was down to 120
psi and the Hall wasn't doing a great deal better. Still, the pair soon
settled down to a steady 10 to 12 mph on the gradient and the sound
effects were quite satisfactory as you can hear in this recording made
as the pair reach the top of the climb at Hemerdon Sidings.
Despite the poor coal the rest of the run to Bristol was accomplished
successfully and without any drama or too much excitement. But at least
we made it.
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4930
& 7819 climbing Hemerdon Bank. 8th April 1985 |
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The next attempt to have a steam hauled run
run from Bristol to Plymouth was made on 7th July 1985. This time motive
power was to be Castle 5051 'Drysllwyn Castle' and Hall 4930 'Hagley
Hall'.
We had been on a railtour the previous day which had not been without
it's problems. The motive power had not been as booked as this train
had been intended to be hauled by the 4-4-0 'City of Truro' which wasn't
ready in time so we had 7029 'Clun Castle' instead and the other loco
involved, 4930, wasn't steaming well. This proved to be due to leaking
tubes. 5051 almost became involved in this railtour as a replacement
for the Hall but it failed with brake problems.
By the following morning both locos had been repaired, the Castle's
brake problem proved to be minor and the Hall's tubes had, apparently,
succumbed to treatment and we were able to depart from Bristol no more
than 30 minutes late.
Time was gained to Taunton where the Hall's tubes were found to be leaking
again but this wasn't thought to be serious enough to cause problems.
Soon after leaving Taunton the Hall's fire began to give cause for concern.
Nothing to do with leaking tubes but clinker. Still we made it to Exeter
and took water and had a photostop at Dawlish Warren. This was followed
by a run along the sea wall in glorious sunshine and yet another water
stop at Newton Abbot from which we departed about 50 minutes late.
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Now for the main event, the South Devon banks.
The chance of getting a run at the ascent of Dainton was denied us by
a track circuit failure at Aller Jc. requiring us to pass a signal at
danger under the control of a hand signal man at a much reduced speed.
Once onto the bank, at first, although the locos did not seem to be
being worked particularly hard but things appeared to be Ok.
By the time we were approaching Stoneycombe where this recording starts,
although speed is low it appears that we are actually going to make
it. Then the Castle, which is on the front of the Hall in correct GWR
practice, loses its feet, is unable to get a grip and continues slipping.
The Hall on the other hand does not slip and can be heard chuffing gently!
Unbeknown to us in the train the Hall's fire had clinkered up once again
and, with boiler pressure and water level very low the crew were considering
stopping for a blow up when the Castle began slipping. Eventually we
come to a stand with the steepest part of the bank still ahead
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An initial attempt to restart the train was
unsuccessful and the crew hand sanded the track for a second attempt
which was also unsuccessful.
Eventually the decision was taken to summon diesel assistance and, in
due course, diesel 50045 arrived having been detached from a service
train standing at Aller Jc. and was coupled on to the rear of the train.
Initial attempts to restart resulted in the diesel suffering an overload
trip but eventually we got under way but had to have a further stop
at the summit at Dainton as the crew on the Hall did not want to proceed
onto the falling gradient beyond for fear of the change in gradient
to causing the low level of water in the boiler uncovering the fire
box crown! At this point the diesel was still in Dainton tunnel and
had to be uncoupled there before it could return to it's train standing
at Aller Jc., one of ten that we had delayed.
Eventually we proceeded down to Totnes where after yet more delay the
tour reversed before returning to London diesel hauled.
After this fiasco it came as no surprise that steam hauled trains were
now banned from running westbound between Bristol & Plymouth!
A week later 5051 & 4930 worked a train back to Bristol but with
steam haulage starting at Newton Abbot, the excuse being 'fire risk'.
It was to be 13 years before I was able to get steam haulage into Plymouth
from on the east!
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5051
& 4930 near Stoneycombe. 7th July 1985 |
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The last 'proper' SSE season
After all the trials and tribulations of GW
150 help was at hand for, on the 9th July 1985 the Scarborough Spa Express
season began. With 22 trains booked to run in the next two months we
had plenty of entertainment to look forward to!
The operation of these trains changed slightly in 1985 with the use
of two locomotives each day, one to cover the morning and evening circles
and another to run from York to Scarborough and back. The cynics amongst
us felt that this was probably just an excuse to increase the running
costs so that the trains would prove uneconomic and could be scrapped
after this year. Sadly, this proved all too true and this was the last
year that 'proper' SSEs ran.
Initially we found that we had a shortage of locos. Some previous performers
were unavailable. Sadly 5305 was out of service undergoing overhaul,
46229 was down at Marylebone and 92220 was away doing GW 150 things
until the end of July. However 4771 'Green Arrow' was expected to be
returned from overhaul at Dairycoates 'any day now'. Indeed, a certain
Humberside loco engineer kept telling us how glad he would be to see
the back of it. He threatened to return it with new nameplates reading
'F***ing Arrer' since that was how it was usually referred to in Hull
having been nothing but trouble since they got it for overhaul! This
meant that the only locomotives available at the start of the season
were the Southern Railway pair King Arthur 4-6-0 777 'Sir Lamiel' and
West Country Pacific 34092 'City of Wells' which was usually turned
out in full Golden Arrow regalia!
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The best part of an SSE from the enthusiast
point of view was the 'Evening Circle' from York via Leeds & Harrogate
back to York, particularly the climb from Leeds to Horsforth and, in
the previous year we had been witness to some remarkable running up
the gradient, generally at 1 in 90 and 1 in 100. On the final train
in 1984 we had had a run in just over 9 minutes Leeds behind 92220 which
we thought pretty well unbeatable.
On the 14th July 1985 34092 'City of Wells' in the very capable hands
of York driver Derek Gell completed the same run in less than 8½
minutes taking just over 5 minutes from Wortley Jc. with a sustained
speed on the gradient of 55 mph. A remarkable performance!
This run proved to be the record for the season and, to the best of
my knowledge has never been bettered. This recording was made passing
through Headingley at a little over 50 mph.
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34092
passing Headingley. 14th July 1985 |
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9F 2-10-0 92220 'Evening Star' returned from
it's GW150 commitments at the beginning of August and was able to take
over from 'City of Wells' which was returning home to the Keighley &
Worth Valley Railway.
On 4th August 1985 the 9F is heard in this recording departing from
York for Scarborough.
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92220
departing from York. 4th August 1985 |
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The V2 4771 'Green Arrow' did actually put
in a rather late appearance on the SSEs and worked for the first time
on 25th August when it was booked for the morning and evening circles.
On arrival back at York after the morning circle the loco was found
to have run a driving wheel axle box hot and took no further part in
the proceedings.
The loco that did most work on the Scarborough Spa Expresses in 1985
was the King Arthur 777 'Sir Lamiel'.
This recording is of the Arthur, the loco that worked on 20 out of 22
days in the course of which covering almost 2300 miles, making a fine
sound passing Headingley during the evening circle of 22nd August 1985.
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777
passing Headingley. 22nd August 1985 |
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Sadly 1985 proved to be the last 'proper' season
of Scarborough Spa Expresses. Our fears about the new area management
at York wanting to show the operation in a bad light economically proved
only too true and, although the Scarborough Spa Express ran in the following
and some subsequent years, it was only been between York and Scarborough
and there has never been a regular operation over the complete route
since.
For myself it was sometimes quite hard to arrange things to be able
to get out on each of the 22 days that the SSE ran each year but I'm
certainly glad that I did.
That I did turn out each day was mainly due to the enthusiasm shown
by the York loco crews, not just drivers but firemen and loco inspectors
too. I always felt that, since they appeared to be doing all this for
me and the other regulars, it would be the height of bad manners not
to be present!
Without them and their enthusiasm for the operation, which built up
over the years it would just not have been the same.
We will never see the like again.
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Steam into Cornwall...
One thing that we did do in 1985 was travel
about a lot! After being in Scotland the previous week, Friday 6th September
1985 saw steam return to the main line in Cornwall for the first time
since the 60's and, of course, the regulars were all there. That's 'all
there' in the physical sense, mentally I'm not so sure.
As part of the GW 150 celebrations 3440 'City of Truro' was booked to
work a train from Plymouth to it's namesake city but, as you might have
guessed, the loco wasn't ready in time so the honour fell to Castle
7029 'Clun Castle'. An early start from Plymouth saw us reach Par without
any difficulty or excitement and not very much noise either.
From Par to Truro the loco worked tender first having turned on the
turntable still in existence at St. Blazey depot not far away. With
7029 back from turning and servicing it sounds like the entire population
of Par has turned out to see us as we depart. And why weren't those
children at school?
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7029
departing from Par. 6th September 1985 |
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...and into West Wales
Another new route saw preserved steam for the
first time on 21st September 1985 when, as part of the GW 150 celebrations
a series of trains were run over the weekend from Swansea to Carmarthen
with Hall 6960 'Raveningham Hall' and Castle 5051 'Drysllwyn Castle'
although the later only worked the last train on the afternoon of the
following day.
I didn't reach Swansea until the Saturday afternoon and was only able
to do the final run to Carmarthen.
I recall meeting another regular on the platform at Swansea who had
done the other trips that day and who took great pleasure in telling
me that, until then, the trash had been tremendous! He then took even
greater pleasure in informing me that for the last trip that day we
were having a change of crew and that the driver taking over was reputed
to be a 'gnome'! Sadly this proved to be the all too true.
The main interest from the point of view of noise was the steep climb
from Swansea to Cockett but this was taken fairly gently by this driver.
Had this run been really good I would have been rather annoyed as, soon
after we started on the climb I was accosted by a very large, very Welsh
lady who insisted that she had to get to the window that I was using
to record from. Since it was obvious that she wouldn't have taken no
for an answer and she was a lot bigger than me I let her. It turned
out that she wanted to wave to her house as we passed! Due to her size
I was unable to see if it waved back.
Eventually I was able to reclaim my window and was in time to record
'Raveningham Hall' reach the top of the 1 in 52 gradient and enter Cockett
Tunnel where the gradient eases.
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6960
approaching Cockett Tunnel. 21st September 1985 |
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Maximum Power!
Throughout the summer of 1985 46229 'Duchess
of Hamilton' had been based at Marylebone and in the capable hands of
the steam drivers there had provided some remarkable performances.
On 5th October 1985 the locomotive travelled north on it's way back
to York to work it's last few trains before coming out for overhaul
and, on this last run out of Marylebone we were hoping for something
special!
During the early stages of the journey, while the running was good enough,
the engine wasn't worked particularly hard. This situation changed dramatically
after High Wycombe.
This recording starts soon after passing through the station, where
there is a speed restriction, at around 30 mph.
Clear of the restriction the driver opens the engine up ready for the
climb to Saunderton.
On gradients never steeper than 1 in 164 speed rose rapidly and, in
just over 2 miles had topped 60 mph. The driver gradually extended the
cut off and speed continued to rise and, after this section of the complete
recording has ended, reaches a little over 72 mph before the regulator
is closed close to the summit.
A truly remarkable performance with a 12 coach load providing us with
one of the highest power outputs ever produced by a steam locomotive
in the UK. We had been hoping for something special and we certainly
weren't disappointed!
The Duchess worked two more trains after this, both over the S&C
before coming out of traffic for an overhaul which, for various reasons
became quite protracted and it wasn't until 1990 that we saw the locomotive
back on the main line.
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46229
after passing High Wycombe. 5th October 1985 |
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Success!
The last Great Western Limited, in connection
with GW 150, ran from Plymouth to Bristol on 27th October 1985.
This run was an extra that had been arranged specially for those who
had suffered the disappointment of the very first train in the series.
The motive power was the same locomotives that had both failed with
hot tender axle boxes on that first run, 7819 'Hinton Manor' & 6000
'King George V'.
I'm glad to be able to report that no similar problems occurred on this
occasion and, indeed, the entire run went very well with some quite
good running at times.
When double heading was called for it was normal GWR practice was for
the smaller pilot engine, in this case 7819, to be coupled behind the
train engine. No other railway did it this way but the GWR believed
that there were just two ways to do things, their way and the wrong
way. However, on this occasion, when we left Plymouth we had 7819 on
the front of the King.
The GW took over during the water stop at Newton Abbot as both locomotives
had to come off the train to reach the watering point the opportunity
was taken to get them back on the train in the right order, with the
King on the front of the Manor in correct GWR practice!
Later, after a crew change and another water stop 6000 & 7819 are
heard departing from Exeter ready for the climb to Whiteball
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6000
& 7819 departing from Exeter. 27th October 1985 |
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Marylebone again.
Steam out of Marylebone was proving to be a
great success and the next visitor to work trains to Stratford should
have been 60009 'Union of South Africa'.
The A4 had worked a train for the SRPS from Kilmarnock to Keighley from
where it continued to York and had been booked to continue south to
take up it's workings out of Marylebone on September 28th.
While at York it was intended that the A4 would have some work carried
out to rectify a problem with its springs. However, the problem was
found to be far more serious than had been anticipated and, eventually
it was decided that, instead of proceeding to Marylebone it would be
going to Doncaster Works instead where facilities were available to
carry out the work.
As they say, it's an ill wind, and while we were disappointed not to
have the A4, we were pleased to discover that the replacement engine
was to be 34092 'City of Wells' which ran, engine and coach down to
London on 1st November to work to Stratford and back on the following
day.
In this recording made soon after the start of the return journey from
Stratford upon Avon, 34092 with 12 coaches behind the tender is just
beginning to climb the 1 in 75 gradient in fine style.
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34092
after departing from Stratford. 2nd November 1985 |
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The V2 at last
After it's much delayed return and subsequent
failure with a hot axle box on the Scarborough Spa Express many were
looking forward to having the V2 2-6-2 4771 'Green Arrow' back on the
main line.
This happened on 9th November 1985 when the loco worked the White Rose
with steam haulage from Sheffield to Manchester then back to York.
Like every other train that had worked this itinerary the V2 suffered
a signal check before being allowed to cross to the Hope Valley line
approaching Dore & Totley. In this recording we hear 4771 recovering
from the check and continuing the 1 in 100 climb towards Totley Tunnel.
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4771
near Dore & Totley. 9th November 1985 |
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Round and round the 'Sub' with Santa
After the success of running Santa Specials
around the Edinburgh Suburban line in 1984 the SRPS decided to repeat
the exercise over the weekend of 14/15th December 1985.
Motive power was, once again, the veteran North British Railway Class
C Goods 0-6-0 673 'Maude'.
This year, unlike 1984, trains ran clockwise around the suburban line.
From a sound recording point of view this was rather a pity as the gradients
in this direction are much less severe than travelling the other way.
Still, once the priming stops, 673 makes a fine sound climbing away
from Portobello Jc.
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673
passing Portobello Jc. 14th December 1985 |
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Black 5 Back
Black 5 5305 just made it back into traffic
after overhaul before the end of the year in time to work a Santa Special
for the Humberside Locomotive Preservation Group from Hull to Scarborough
and back on 28th December 1985.
After an excellent climb of Bridlington Bank we were checked by signals
approaching Filey, presumably while the signalman closed the gates on
the level crossing beyond the station. Eventually the signals clear
and 5305 begins to accelerate through the station and on towards Scarborough
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5305
passing Filey. 28th December 1985 |
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102.3?
One of the locomotives most looked forward
to in connection with GW 150 was the 4-4-0 3440 'City of Truro'. As
you will have read in notes to previous recordings this locomotive had
been booked for various trains throughout the year but had never been
ready in time to take up it's booked workings.
At last, in late October, the locomotive was ready for it's first main
line passenger run. This was advertised originally for 13th October
but actually ran a week later on 20th because, surprise, surprise, the
engine wasn't ready for the earlier date. The booking form for this
tour said that it was 'a rare opportunity to spend an afternoon in the
West Country with 3440'. And the bargain fare for this outing? Just
£45! Which, to be fair, did include Lunch and Dinner.
After much speculation, because the route and destination for this first
run was supposed to be kept secret, we discovered that the route for
this train was going to be Gloucester to Newport and back. Hardly West
Country!
Under the circumstances it was hardly surprising that the train attracted
less than 100 passengers, which of course did not include me!
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So it was that my first opportunity to ride
behind the engine came on the final main line steam trip of the year
on 30th December 1985. This was yet another Santa Special, this time
from Kidderminster to Hereford and back and with 'City of Truro' we
also had 4930 'Hagley Hall'.
On the climb into the Malvern Hills we were stopped by signals at Malvern
Wells awaiting a train clearing the single track section that begins
there.
With the section clear the pair restart on the 1 in 80 gradient while
a spectator's dog sounds to be trying to get in on the act!
But hark! What is that high pitched whistling sound that we can hear?
No, surely not! It couldn't be, could it? But it was. When we stopped
at Ledbury a little later it came as no great surprise to us in the
train when it was found that an axle box on the Hall's tender had run
hot. We proceeded from there to Hereford at reduced speed with the prospect
of a diesel hauled run back to Kidderminster to look forward to.
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3440
& 4930 at Malvern Wells . 30th December 1985 |
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We were booked to have a break of about 90
minutes at Hereford while the engines were turned and serviced but,
since they had decided to try to get the Hall fit for the return journey
and we had been quite late arriving it was well after dark when steam
was seen approaching from the north and we discovered that the Hall
had been repaired and that we were to have a steam hauled run back to
Kidderminster after all.
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This final main line steam trip for 1985 saw
the end of what, for me proved to be my busiest year for main line steam
during which I travelled behind steam on the main line on no less than
77 days, covering a little less than 12,000 miles behind 22 different
locomotives and paying far more than I could really afford for the privilege.
If 1986 had proved as busy I would have been penniless by the end of
the year!
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